TWO DAY WORKSHOP RESULTS
SET UP TIME
Before
After
Reductions
1. Press
3hrs 20 mins
45 mins
78%
2. Canning
1hr 45 mins
23 mins
78%
3. Capper
58 mins
15 mins
75%
4. Extruder
32 mins
6 mins
80%
5. P.C.B. Line
1hr 10 mins
5 mins 30 secs
91%
CELLS   Before   After
* LT
**WIP
***OPS
LT
WIP
OPS
1. Metal Ass'y
6hrs
8500
5
10secs
8
3
2. Lock
48hrs
10,000
5
17secs
10
3
3. Bowl
25hrs
600
4
90secs
15
2
4. Textiles
6 days
3,000
15
1hr 30mins
30
6
5. Slippers
3 weeks
10,000
5
48secs
10
4
* LT - Lead Time **WIP - Work in Progress ***OPS - Operators
TPM Downtime Reduction Defects Reduction
1. Press
63%
46%
2. Wrapping Mchn.
48%
31%
3. Rim Line
32%
60%
4. Strip
58%
52%
5.Plastic Extruder
72%
60%
KAIZEN
1. Ladle faults saving £50,000 per year
2. Bottle damage -60%
3. Order lead time 4 days to 3hrs
4. Moulding wastage saving £35,000 per year
5. Friction stay production increase 800/hr to 1200/hr
POKA-YOKE - 'O' DEFECTS
1. Lock Manufacture
2. Strip
3. Control Assembly
4. Electronic Assembly

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